2.1.1 Narrative
Actions to remove debris and oil from the well and then to properly plug the well are underway. See prior POLREPs.
2.1.2 Response Actions to Date
See Prior POLREPs for activities through April 21, 2016. Removal of oil and debris from the well continues. Oil and gas continue to be encountered indicating that the EPA activity of Fall 2015 was not successful at preventing the discharge of oil and gas from the facility.
The owner of the building continues to assist EPA.
During this period, the brush plug encountered last week was finally cleared at a depth of about 950. A bridge was also encountered and drilled on 4/27/2016 at a depth of about 980 feet. A release of gas was noticed after the bridge was cleared. Afterwards the drill stem was easily dropped to a depth of about 1043 feet requiring the purchase of additional drilling rods.
On April 28, towards the end of operations for the week, drilling activities encountered another wooden bridge plug at a depth of 1085 feet.
Response personnel evaluated the available information about the well. Nearby wells were recorded or observed to be between 1000 and 1100 feet in depth to encounter "Big Injun" oil formation. According to an evaluation of other wells in the area, the oil formation "pay zone" is somewhere within a unit of rock which is up to 275 feet thick. As such, and considering all available information, operations may encounter the bottom of the well at about 1240 feet.
The AreaRAE system continues to identify detections of VOCs above the alarm level. Most of these detections continue to relate to instances during which the equipment was being fueled or when the engines were started or adjusted.
2.1.3 Enforcement Activities, Identity of Potentially Responsible Parties (PRPs)
See Prior POLREPs.
WVDEP located records for the well (and 2 other nearby wells). The records indicated the well owner to be C.G. Broaddus and that the well was plugged. The plugging affidavit indicated that casing pipes were pulled from the well and the well was plugged in a manner prescribed by the State in 1949. The OSC originally believed that plugging did not occur due to the discovery of the 2 inch tubing and sucker rods in the well at about 35 feet. However, it has subsequently been determined that the well had indeed been plugged, but in a manner not documented on the plugging affidavit.
The OSC examined court records and consulted a civil investigator. There is no record of the whereabouts of C.G. Broaddus.
2.1.4 Progress Metrics
The table below reflects disposal from the Site through April 21, 2016
Waste Stream |
Medium |
Quantity |
Manifest # |
Treatment |
Disposal |
oil |
solids |
4 - 55-gallon drums |
|
|
X |
oil |
oily liquids |
4364 gallons |
|
|
X |
oil |
oil solids |
2 tons |
|
|
X
|
|