U.S. ENVIRONMENTAL PROTECTION AGENCY
POLLUTION/SITUATION REPORT
BP Terminal Indianapolis - Removal Polrep

UNITED STATES ENVIRONMENTAL PROTECTION AGENCY
Region V
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Subject:
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POLREP #35
Progress Report
BP Terminal Indianapolis
Indianapolis, IN
Latitude: 39.8027163 Longitude: -86.2160273
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To:
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From:
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Paul Atkociunas, On-Scene Coordinator
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Date:
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8/18/2014
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Reporting Period:
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June 17 to August 14, 2014
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1. Introduction
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1.1 Background
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Site Number: |
Z5K6 |
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Contract Number: |
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D.O. Number: |
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Action Memo Date: |
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Response Authority: |
OPA |
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Response Type: |
PRP Oversight |
Response Lead: |
PRP |
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Incident Category: |
Removal Action |
NPL Status: |
Non NPL |
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Operable Unit: |
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Mobilization Date: |
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Start Date: |
11/14/2011 |
Demob Date: |
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Completion Date: |
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CERCLIS ID: |
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RCRIS ID: |
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ERNS No.: |
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State Notification: |
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FPN#: |
E11504 |
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Reimbursable Account #: |
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1.1.1 Incident Category
Manufacturing/processing/maintenance - oil and gas storage
1.1.2 Site Description
The BP Indianapolis Terminal (the site) began operating as a petroleum storage and distribution facility since 1941. The site consists of an administrative building, service garage, petroleum distribution rack, miscellaneous warehouse and pumping station sheds, oil/water separator, underground storage tanks (UST) and aboveground storage tanks (AST), which contain gasoline, diesel, ethanol, furnace oil, and heating oil. AST capacity ranges from 672,000 to 3,360,000 gallons, with a total capacity exceeding 18,000,000 gallons.
1.1.2.1 Location
The site is a 41-acre bulk terminal located at 2500 North Tibbs Avenue in Indianapolis, Marion County, Indiana, 46222. Site coordinates are 39.8027163 degrees north latitude and 86.2160273 degrees west longitude. The site is bordered by commercial property to the north; shopping plaza to the northeast; Ferguson Industrial Plastics Division and a fire station to the east; undeveloped property to the south; and Little Eagle Creek to the west.
1.1.2.2 Description of Threat
Environmental investigations conducted by BP and its consultants documented that there are petroleum-related groundwater impacts from benzene, toluene, ethylbenzene, xylenes (BTEX), methyl tertiary butyl ether (MTBE), naphthalene, ethanol, and polynuclear aromatic hydrocarbons (PAH) including benzo(a)anthracene, benzo(a)pyrene, benzo(k)fluoranthene, chrysene, dibenz(a,h)anthracene, and indeno(1,2,3-cd)pyrene beneath the site. Light Non-Aqueous Phase Liquid (LNAPL) and dissolved-phase contamination have been found in a shallow aquifer beneath the Site and at seeps along Little Eagle Creek.
1.1.3 Preliminary Removal Assessment/Removal Site Inspection Results
Refer to previous Pollution Reports (PolRep).
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2. Current Activities
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2.1 Operations Section
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2.1.1 Narrative
The site was previously in the Voluntary Remediation Program (VRP) of the Indiana Department of Environmental Management (IDEM). IDEM referred the site to the U.S. Environmental Protection Agency (EPA) on December 13, 2010. On November 14, 2011, EPA executed an Administrative Order by Consent (AOC) under Section 311 of the Clean Water Act. The AOC requires BP to implement removal measures to prevent migration of petroleum hydrocarbon impacted groundwater into Little Eagle Creek.
2.1.2 Response Actions to Date
During the reporting period, BP conducted the following actions:
- Continued maintenance on the groundwater extraction and treatment system (GWET)
- Conducted the monthly manual light non-aqueous phase liquid (LNAPL) recovery on on June 16 and July 18, 2014
- Conducted the monthly Little Eagle Creek surface water sampling event on June 16 and July 18, 2014.
- Conducted a bail-down test on August 4, 2014 to obtain data to evaluate the transmissivity of LNAPL present in DHW-44.
2.1.3 Enforcement Activities, Identity of Potentially Responsible Parties (PRPs)
EPA executed Docket No. V-W-11 C-984, an AOC with BP on November 14, 2011.
2.1.4 Progress Metrics
Below is a schedule of items included in the AOC. On August 14, 2104, EPA approved a Revised LNAPL Recovery Operations and Maintenance Plan; the plan and approval letter can be located in the Documents Section of the website outlined below.
Milestone |
Date Due |
Date Done |
Effective Date (ED) |
11/14/2011 |
11/14/2011 |
LNAPL Recovery, Quarterly Creek & MW Sampling |
11/14/2011 |
11/14/2011 |
Contractor Notification |
11/21/2011 |
11/21/2011 |
Project Coordinator Notification |
11/21/2011 |
11/21/2011 |
HASP Submittal |
12/6/2011 |
12/6/2011 |
QAPP Submittal |
12/6/2011 |
12/6/2011 |
HASP/QAPP Approval (HQA) |
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1/5/2012 |
HASP/QAPP Revisions |
1/13/2012 |
1/13/2012 |
LNAPL Recovery, Creek Sampling Locations Notification, Quarterly MW Sampling |
1/27/2012 |
1/27/2012 |
Creek and Groundwater Sampling Locations Revisions |
2/17/2012 |
2/21/2012 |
Creek Sampling Location Approval (CS) |
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2/21/2012 |
Monthly Creek Sampling |
3/6/2012 |
3/6/2012 |
On-Site Construction |
12/14/2011 |
8/30/2011 |
Construction Complete |
3/19/2012 |
3/19/2012 |
Investigation Work Plan |
2/12/2012 |
2/12/2012 |
Revised Work Plan |
4/13/2012 |
4/13/2012 |
Investigation Complete (IC) |
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- Supplemental soil characterization |
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6/18/2012 |
- Supplemental groundwater characterization |
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6/22/2012 |
- Supplemental surface water characterization (normal flow) |
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10/8/2012 |
- Supplemental surface water characterization (low flow) |
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6/27/2012 |
- Supplemental sediment characterization |
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6/27/2012 |
- Natural Resources Assessment |
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8/19/2013 |
- Sediment toxicity testing and analysis (benthic testing) |
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8/19/2013 |
- Aquifer testing |
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10/20/2012 |
Investigation Report |
1/28/2013 |
1/28/2013 |
Investigation Report Approval (IRA) |
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1/21/2014 |
Removal Work Plan |
3/24/2014 |
3/24/2014 |
Removal Work Plan Approval (RWA) |
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6/9/2014 |
Removal |
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Final Report, 60 days after removal is complete |
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2.2 Planning Section
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2.2.1 Anticipated Activities
The following sections discuss planned response activities and next steps.
2.2.1.1 Planned Response Activities
During the next reporting period, BP will:
- Continue to provide oversight and documentation support to EPA's On-Scene Coordinator (OSC);
- Perform Little Eagle Creek monthly surface water sampling; and
- Continue monthly LNAPL recovery and system operation & maintenance (O&M).
2.2.1.2 Next Steps
BP will proceed with the implementation of the Revised Removal Work Plan in accordance with the schedule outlined in Section 8 of the approved plan. The Final Design of the Modified GWET System is due 90-days following the Approval of the Removal Work Plan.
2.2 Issues
During the reporting period, the pump and treat system was operational 90.3% of the time. The following unscheduled down times occurred:
- On June 11, 2014, an LEL alarm caused the system to shut down. Follow-up monitoring with a 4-gas meter did not confirm the presence of elevated LEL atmosphere in the enclosure. Further, the system data was analyzed and no LEL measurements of greater than 10% were recorded. No specific cause for the shutdown was identified. The system was down for five (5) days and will be continued to be monitored.
- On June 24, 2014, a storm postponed work causing the system to be left down for the night. O&M activities were concluded on June 25, 2014 and the system was turned back on.
- On July 11, 2014, the system was shut down to repair a corroded pipe. O&M activities were concluded on July 14, 2014 and the system was turned back on.
- On August 7, 2014, an LEL alarm caused the system to shut down. Follow-up monitoring with a 4-gas meter did not confirm the presence of elevated LEL atmosphere in the enclosure. Further, the system data was analyzed and no measurements greater than 5% were recorded. No specific cause for the shutdown was identified. The system will continue to be monitored. The system was returned to service within one day.
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2.3 Logistics Section
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Not applicable (NA)
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2.4 Finance Section
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No information available at this time.
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2.5 Other Command Staff
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2.5.1 Safety Officer
BP is conducting all environmental work at the site under an approved Health and Safety Plan (HASP).
2.6 Liaison Officer
NA
2.7 Information Officer
NA
2.7.1 Public Information Officer
NA
2.7.2 Community Involvement Coordinator
NA
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3. Participating Entities
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3.1 Unified Command
NA
3.2 Cooperating Agencies
IDEM
Marion County Public Health Department
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4. Personnel On Site
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NA
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5. Definition of Terms
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AOC |
Administrative Order by Consent |
AST |
Aboveground Storage Tank |
BTEX |
Benzene, toluene, ethylbenzene, xylenes |
EPA |
Environmental Protection Agency |
FPN |
Federal Project Number
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GWET
HASP |
Groundwater Extraction and Treatment System
Health and Safety Plan |
IDEM |
Indiana Department of Environmental Management |
LNAPL |
Light Non-Aqueous Phase Liquid |
MTBE |
Methyl teriary butyl ether |
NA |
Not Applicable |
O&M |
Operation and Maintenance |
OSC |
On-Scene Coordinator |
PAH |
Polynuclear aromatic hydrocarbons |
PolRep |
Pollution Report |
PRP |
Potentially Responsible Party |
START |
Superfund Technical Assessment and Response Team |
UST |
Underground Storage Tank |
VRP |
Voluntary Remediation Program |
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6. Additional sources of information
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6.1 Internet location of additional information/report
Additional information can be found at www.epaosc.org/bpterminalindy.
6.2 Reporting Schedule
The OSC will submit the next PolRep on or about September 17, 2014
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7. Situational Reference Materials
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NA
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